Successful U-joint replacement on a 528e!
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Successful U-joint replacement on a 528e!

 
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Steve Richfie1d
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Posted: Tue Nov 15, 2005 9:13 am    Post subject: Successful U-joint replacement on a 528e! Reply with quote

It appears that one of the main reasons that older BMWs are scrapped is
that their tiny U-joints fail, which often costs ~$1,000 to have replaced!

After reading all of the reports about the impossibility of changing
U-joints on BMWs, we (my son and I) decided to give it a try with
relatively primitive tools. Our efforts were quite successful, as we
have no vibration even at freeway speeds and then some. I thought that I
would share our method so that others can fix their own BMW U-joints for
~$20.

The most time consuming part was removing the old U-joint, because there
is no way to press it out! Also, you should be careful to support the
holders so you don't squeeze them together too hard and distort them.
This is how we removed them:

1. If you look closely, you'll see that the bearings are "staked" to
hold them in place with no possibility of removal. We cut out the stakes
with our Dremmel with an abrasive cutoff wheel, cutting into both the
bearing and the housing to get it all and then some to make sure that
things didn't jam during the following steps. Don't be afraid of making
a mess of things, because the extra grooves you cut will HELP at the end
of this project! When we got ours apart, we could see that we hadn't
gotten all of the stakes, probably adding tons to the pressure we needed
to get it apart. Don't forget to mark the relative position of the two
bearing holders so you can get them back the way they were when you
reassemble things, which will probably help to preserve balance.

2. The first bearing we did by supporting the most destroyed bearing
with a large enough socket for the bearing to enter it, and hammering on
a socket placed on the opposite bearing. While this cannot completely
remove the bearing, it can allow it to exit far enough that you can cut
a giant X on the end with a Dremmel with an abrasive cutter, jam a large
screwdriver in, and pry it out as its sides collapse where they were
chewed up by the spider. With luck you can get the whole thing out this
way, but all that is really necessary is that you completely expose the
end of the spider for removal in the following step.

3. Turn the drive shaft over, put a smaller socket onto the end of the
spider and the large socket on the opposite bearing and hammer it out as
far as it will go. Then, you should be able to remove the spider from
the end piece that held the two bearings. Place a socket that is just
slightly smaller than the OD of the second bearing onto the inside of
holder, attach an extender that passes through the hole you cut in the
first bearing, and hammer out the second bearing. Once it is out, if you
failed to get the first bearing out in step 1, then just turn the drive
shaft over and hammer it out the same way.

4. You can do the other two bearings the same way, or you can now
"cheat" like we did and simply cut the spider into thirds to remove it,
cut the end out of one of the bearings, and proceed as in step 2 above.
If you decide to cut the spider, you'll need a mean-business cutoff tool
of some sort, because it is hardened steel. We used an angle grinder.
Once the spider if out, you'll still need to punch a hole in one of the
bearings to pass your extender through to hammer out the opposite
bearing, then turn the drive shaft over and remove the bearing with the
hole.

5. Now you'll want to clean up any of the stakes you failed to remove in
step 1, and if the spider has chewed up the housing you may want to get
it fixed, e.g. at a machine shop. However, JB Weld probably works as
well, just put some of that in there immediately prior to assembly and
complete the job before it hardens. However, we just ignored the problem
and that also seemed to work!

6. Assembly is straightforward. Add LOTS of grease and just press one
bearing in a ways, insert the spider into it, press the opposite bearing
in a ways, center the spider into both of them, and proceed pressing
both bearings in. BE CAREFUL because there is no correcting errors, as
you'll have to just cut your mistakes out like you did the old bearings
and start over with another new U-joint. We found that the correct
position was VERY close to being equally deep on both sides, so use a
depth gage and alternatively tap the bearings in until they are both in
contact with the spider at about the same depth. Once all bearings are
in approximately equal distances ...

7. Construct an alignment jig. Ours consisted of a dining room table
with the extra leaf in, two egg cartons, and a piece of 2x4 cut into an
L shape. Trim the egg cartons to support the drive shaft at the balance
points of each segment, so that you can turn it without hitting the
balance weights or it wobbling. The L-shaped 2x4 should rest flat on the
table, clear the end bolts, and contact the flat machined end of the
U-joint, with the top of it being just barely below the top of the
machined surface. Attach some masking tape to the top of the 2x4 to
write on.

8. Now for the fun! Push the 2x4 up against the end of the U-joint
assembly to force it into full contact with the 2x4 and mark where the
machined protrusion just crosses the top of the 2x4. Note that a small
change in height makes a large change in the distance between the two
points where the protrusion crosses the top of the 2x4. Check this at
several points to establish where the protrusion is high, and hammer on
the appropriate bearings while backing up the opposite bearings with
something HEAVY to adjust their depth, until you can no longer detect
ANY change in the height of the protrusion as you rotate the drive
shaft. I estimate that this method can give you approximately 0.005"
accuracy, whereas a good drive line lathe can give you maybe 0.002"
accuracy. No, egg cartons are not as good as fine machinery, but they
ARE good enough for this job.

9. Now that it is all back together and aligned, clean up the ends VERY
thoroughly to remove all grease, put a drop of Thread Lock on each
bearing, followed by a bunch of JB Weld to hold things in place. Set it
aside for several hours to harden, rotating it every few minutes to keep
the JB Weld from drooping until it hardens sufficiently.

10. Give it a day for the JB Weld to harden before you drive it.

If you have any questions, please email us directly as we don't usually
monitor this group. Don't forget to remove the NOSPAM from our email
address.

Lotsa luck.

Steve and Ed Richfie1d

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Dave Plowman (News)
Guest





Posted: Tue Nov 15, 2005 5:21 pm    Post subject: Re: Successful U-joint replacement on a 528e! Reply with quote

In article <3ttlhmFtk08cU1@individual.net>,
Steve Richfie1d <Steve@NOSPAM.smart-life.net> wrote:
Quote:
It appears that one of the main reasons that older BMWs are scrapped is
that their tiny U-joints fail, which often costs ~$1,000 to have
replaced!

Doesn't anyone do reconditioned prop shafts? The snag with bodging out
staked bearings rather than machining is the likelihood of poor
balance/out of true afterwards. The correct way is to machine out the
staking and machine grooves to take clip in ones - then rebalance.

--
*If horrific means to make horrible, does terrific mean to make terrible?

Dave Plowman dave@davenoise.co.uk London SW
To e-mail, change noise into sound.
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admin
Guest





Posted: Tue Nov 15, 2005 9:03 pm    Post subject: Re: Successful U-joint replacement on a 528e! Reply with quote

Steve Richfie1d wrote:
Quote:
Lotsa luck.

Steve and Ed Richfie1d

Steve and Ed..

This is simply wonderful! This is what the "Hack Mechanic" should be in
Roundel. Real hack answer to a real problem. I'd never have thought of
JB Weld to hold the bearings in place, but no reason it wouldn't work.
The forces aren't huge and JB Weld can hold most anything together I've
ever tried it on.

Wonderful - thanks for posting it!

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Steve Richfie1d
Guest





Posted: Wed Nov 16, 2005 9:13 am    Post subject: Re: Successful U-joint replacement on a 528e! Reply with quote

Dave,

Quote:
It appears that one of the main reasons that older BMWs are scrapped is
that their tiny U-joints fail, which often costs ~$1,000 to have
replaced!

Doesn't anyone do reconditioned prop shafts?

Sure. It takes a lot of time to do this, and then there isn't any
guarantee that the center bearing doesn't also have problems. There is a
guy on eBay who will change U-joints for ~$400, which is probably a fair
price considering the time and frustration involved in doing it yourself.

Quote:
The snag with bodging out
staked bearings rather than machining is the likelihood of poor
balance/out of true afterwards.

Looking at my driveline, there is a large balance weight welded to the
tail end of the driveline tube. My best guess was that it was there to
compensate for the errors in the ORIGINAL installation, and so it
probably just contributes problems once the bearing has been changed.

Quote:
The correct way is to machine out the staking

Can't be done, because the edge of the bearing is rounded and the
staking conforms to this rounding. There is NO WAY to get a mill cutter
into this tight place to remove this material. This seems to require the
services of some sort of circular cutter like the edge of a Dremmel
wheel. Even then, you must cut out some bearing and some of the holder
to get enough to remove the bearing.

and machine grooves to take clip in ones

This would be pretty tricky. A U-joint that is completely missing its
bearings only causes a centration error of around 0.050 while shaking
the car rather noticeably. A clip would need to hold it VERY accurately,
which would require some pretty tricky machining. Remember, the bearing
is really hard, so making a groove with a tiny circular saw would
destroy the saw if you cut too close, and any clearance you leave
directly translates into centration error when it is assembled. Further,
any extra groove width would also translate into centration error.

- then rebalance.

Yes, a nice idea if you have the equipment to do this. However, we had
no problems with the driveline as we assembled it, without rebalancing.

Steve Richfie1d
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Steve Richfie1d
Guest





Posted: Wed Nov 16, 2005 9:13 am    Post subject: Re: Successful U-joint replacement on a 528e! Reply with quote

Admin,

Quote:
This is simply wonderful! This is what the "Hack Mechanic" should be in
Roundel. Real hack answer to a real problem.

"Bush mechanic" approaches aren't our usual style except in cases of
recovering vehicles from remote locations, but the perfectly awful
design of the BMW (and I've heard that Datsun does the same thing)
U-joints seemed to preclude other more "professional" approaches.

Quote:
I'd never have thought of
JB Weld to hold the bearings in place, but no reason it wouldn't work.
The forces aren't huge and JB Weld can hold most anything together I've
ever tried it on.

This was the topic of some discussion between Ed and I. After beating on
the bearings pretty hard with a hammer (and a socket to put the force
exactly where it was needed) to adjust their positions, it seemed crazy
to me to think that they would ever shift in service, so I was all for
just putting the driveline back into the car with nothing more to hold
the bearings in position besides the friction of their having been
pressed there. Some front end components are also pressed into place
with no retainers, and they can experience much higher stresses.
However, Ed *REALLY* didn't want to revisit this repair (including
ripping out the exaust system, etc.) and he was willing to do just about
anything to assure that it stayed together, so he volunteered to
degrease the area and glop the JB Weld in place as a sort of
belt-and-suspenders approach to seeing that it stayed together. I
suspect that its primary value is psychological, which is often an
important consideration in bush mechanic repairs, second only to
actually working. Was the JB Weld REALLY necessary? We'll probably never
know for sure.

Quote:
Wonderful - thanks for posting it!

This was a sort of humanitarian duty to all of the BMWs that would
otherwise probably be scrapped for want of a U-joint. It took several
hours of frustrating work, but it sure beats spending upwards of $1,000
because of a bad $20 part.

Steve Richfie1d
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Dave Plowman (News)
Guest





Posted: Wed Nov 16, 2005 7:27 pm    Post subject: Re: Successful U-joint replacement on a 528e! Reply with quote

In article <1132165819.755383.38750@o13g2000cwo.googlegroups.com>,
C.R. Krieger <88.535is@gmail.com> wrote:
Quote:
Not for those of us who know we can buy good reconditioned ones with
all new parts (including center bearing and replaceable U-joints),
balanced, with a guarantee, for ~$400.

That sounds more like it.

--
*If God dropped acid, would he see people?

Dave Plowman dave@davenoise.co.uk London SW
To e-mail, change noise into sound.
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C.R. Krieger
Guest





Posted: Thu Nov 17, 2005 12:30 am    Post subject: Re: Successful U-joint replacement on a 528e! Reply with quote

Steve Richfie1d wrote:
Quote:
It appears that one of the main reasons that older BMWs are scrapped is
that their tiny U-joints fail, which often costs ~$1,000 to have replaced!

Not for those of us who know we can buy good reconditioned ones with
all new parts (including center bearing and replaceable U-joints),
balanced, with a guarantee, for ~$400.
--
C.R. Krieger
(Been there; knew that)
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Steve Richfie1d
Guest





Posted: Sun Nov 20, 2005 9:13 am    Post subject: Re: Successful U-joint replacement on a 528e! Reply with quote

C.R. Krieger,

Quote:
Not for those of us who know we can buy good reconditioned ones with
all new parts (including center bearing and replaceable U-joints),
balanced, with a guarantee, for ~$400.

Still a lot of money to replace a ~$20 part. I guess it really boils
down to what your time is worth. I don't know about you, but I can put
in several frustrating hours to save nearly $400.

Steve Richfie1d
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KMS - Brett Anderson
Guest





Posted: Tue Nov 29, 2005 9:14 am    Post subject: Re: Successful U-joint replacement on a 528e! Reply with quote

But you did so with a huge gamble that's still playing out.

What if you'd put in several frustrating hours, and the result was no better
than the original problem. Then what? Another "several frustrating hours"
trying again?

I applaud you for you're inginuity on this job, but for most people, the
effort/risk is not worth the ~$400 you'd be charged by a professional shop
like Beyer Motorwerks (www.beyermotorwerks.com).


Brett Anderson
www.bmwdiffs.com
Koala Motorsport


"Steve Richfie1d" <Steve@NOSPAM.smart-life.net> wrote in message
news:3uahh1F1057t2U1@individual.net...
Quote:
C.R. Krieger,

Not for those of us who know we can buy good reconditioned ones with
all new parts (including center bearing and replaceable U-joints),
balanced, with a guarantee, for ~$400.

Still a lot of money to replace a ~$20 part. I guess it really boils
down to what your time is worth. I don't know about you, but I can put
in several frustrating hours to save nearly $400.

Steve Richfie1d
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